P4P slow Gimbal action

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I am comparing 2 P4P drones (one white and one obsidian). The gimbal on the white one acts very different and a lot slower than the other one. I have reset and verified all gimbal parameters but still when flying the gimbal recovers from the AC turning rather slow. It takes about 1-2 seconds to get back to a horizontal view. This leads to tilted horizons in the video. You might even become 'seasick'.
What kind of things can I do or verify ?

thanks
Erwin
 
The problem is most likely in the gimble speed adjustments. They can be changed in the GO 4 app depending on the results you seek, mostly for filming but also flying comfort. A quick youtube search will explain the how-to.
 
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Thank you both for the suggestions.

After a factory reset the gimbal speed adjustments should also be reset and the same for the other drone that I compared it with. I have done all resets and all (auto) calibration steps. I found a gimbal rebuild error on my part and corrected that. But the result is still a very slow return to horizontal. I will again take apart the whole assembly and verify if I have not compromised the gimbal yaw motor when doing my repair. It is indeed the camera/gimbal from a crashed drone.

When new results are available I will post these here.
 
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