According to the data, the motors were on until 92 Seconds. That does not mean however that they were spinning. Would need the .dat file from the AC to see that.
According to the data, the motors were on until 92 Seconds. That does not mean however that they were spinning. Would need the .dat file from the AC to see that.
View attachment 96908
Phantom was still powered on?Yes battery was fine. After crash powered down then back up with no problems.
The Phantom has produces 2x .dat files both with the same time, one 111mb one 6.43mb. which one is it?According to the data, the motors were on until 92 Seconds. That does not mean however that they were spinning. Would need the .dat file from the AC to see that.
View attachment 96908
The Phantom has produces 2x .dat files both with the same time, one 111mb one 6.43mb. which one is it?
The .dat files begin at power up, so there could be several. I would try both to start with.
I’ll run them through djilogs and post the excel files tomorrow
The log file reads like a really bad nightmare. I cannot untangle the series of events but, if you consider the entire power up, which was more than one motor start and takeoff, things started to go bad very early on. At 18 s (during the first flight) the GPS stops reporting with an update rate error. The GPS time and location never changes after that, even though the IMU apparently continues to try to update position. At 273 s, during the second flight, the IMU stops reporting position and at 275 s all IMU reporting seems to end.
View attachment 97122
Looking at the end of the data stream shows the motor behavior. The motors simply spool down when the IMU quits, resulting in an uncontrolled descent with the motors idling.
View attachment 97123
I've never seen anything quite like that - the IMU operating system looks like it simply froze. The final log status entries make sad reading. The final line is particularly potent.
251.058 : 21556 [Ctrl<3>] REQ_NAVI_MISSION NAVI_WP_MISSION ctrl_navi_waypoint_mission
251.120 : 21559 WP Mission: received idle vel cmd 5.600000 from app
251.120 : 21559 WP Mission: ack idle vel 0 to app
252.258 : 21616 [Ctrl<1>] REQ_RC_NORMAL ATTI ctrl_atti
252.680 : 21637 WP Mission: received idle vel cmd 5.600000 from app
252.680 : 21637 WP Mission: ack idle vel 234 to app
258.233 : 21914 gps update rate err
258.258 : 21916 [Ctrl<1>] REQ_RC_NORMAL ATTI_HOLD ctrl_gps_atti
260.258 : 22016 [Ctrl<10>] REQ_RC_GO_HOME AUTO_LANDING_HOLD ctrl_auto_landing
261.258 : 22066 [Ctrl<1>] REQ_RC_NORMAL ATTI ctrl_atti
265.258 : 22266 [Ctrl<10>] REQ_RC_GO_HOME AUTO_LANDING_HOLD ctrl_auto_landing
266.258 : 22316 [Ctrl<1>] REQ_RC_NORMAL ATTI ctrl_atti
267.258 : 22366 [Ctrl<10>] REQ_RC_GO_HOME AUTO_LANDING_HOLD ctrl_auto_landing
268.233 : 22414 gps update rate err
270.258 : 22516 [Ctrl<1>] REQ_RC_NORMAL ATTI ctrl_atti
271.258 : 22566 [Ctrl<10>] REQ_RC_GO_HOME AUTO_LANDING_HOLD ctrl_auto_landing
273.958 : 22701 [Ctrl<12>] REQ_AIRPORT_LIMIT AUTO_LANDING_HOLD ctrl_auto_landing
274.138 : 22710 [LED] changed: fly limit,eg:airport
274.258 : 22716 [Ctrl<12>] REQ_AIRPORT_LIMIT AUTO_LANDING ctrl_auto_landing
277.158 : 22861 [LED] changed: no atti
278.233 : 22914 gps update rate err
279.138 : 22960 [M. Stop]ACT.landing
279.138 : 22960 Motor Start 2 Total 125.90
279.138 : 22960 CTRL reset all by motor stopped
279.138 : 22960 [ACT.msg] ACT_AUTO_LANDING can't exec auto-landing while motor off
So look like IMU problem?
@Phantomndmore, I thinking you should do some test flights low to the ground with DJI-GO, (If want to have a claim with DJI). Post a few more logs. Another thought, you still older flights on the Phantom, there maybe some information in those?
Rod
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