urgno said:rfernandez
can you please send me the magic profile ?![]()
thanks a lot
Odd. It says Public on YouTube when I go to settings.SilentAV8R said:Video is marked as Private in YouTube
jonesk32 said:Tonight I worked on the gimbal settings some more. On the test flight the video looks very good to me until around the 2:50 mark when the camera started bouncing and wouldn't tilt the camera over most of the range. At one point I landed, turned off the phantom and the bouncing and tilt issue started almost immediately. I don't know what happened, any ideas?
http://youtu.be/GhMzgigg9ik
amrflyingdude said:jonesk32 said:Tonight I worked on the gimbal settings some more. On the test flight the video looks very good to me until around the 2:50 mark when the camera started bouncing and wouldn't tilt the camera over most of the range. At one point I landed, turned off the phantom and the bouncing and tilt issue started almost immediately. I don't know what happened, any ideas?
http://youtu.be/GhMzgigg9ik
Can you post your PID and power settings? Seems to me too much D and Low P
jonesk32 said:amrflyingdude said:jonesk32 said:Tonight I worked on the gimbal settings some more. On the test flight the video looks very good to me until around the 2:50 mark when the camera started bouncing and wouldn't tilt the camera over most of the range. At one point I landed, turned off the phantom and the bouncing and tilt issue started almost immediately. I don't know what happened, any ideas?
http://youtu.be/GhMzgigg9ik
Can you post your PID and power settings? Seems to me too much D and Low P
Roll: P=10, I=.1, D=19, Power=110, Invert=Blank, Num.Poles=14
Pitch: P=10, I=.1, D=19, Power=90, Invert=Blank, Num.Poles=14
I must not have hit write on my changes, I thought that I had decreased the power 5% as a start with the lighter and better balanced mount. I hadn't touched PID settings, I was hoping to stick with what was in the profile for PID.
amrflyingdude said:Try these and let me know:
Roll: P=10, I=.1, D=16, Power=120, Invert=Blank, Num.Poles=14
Pitch: P=10, I=.0.08, D=17, Power=100, Invert=Blank, Num.Poles=14
rfernandez said:We have been working on another profile and were still tweaking to make sure it works. we will keep you updated. fi you wan the the profile I've been sending out just PM me and i will send it you
I would try raising the basic vertical gain. Id follow the process but you'll probably end up at about 200.Raymond.HK said:I am worried since no other persons seem to have posted similar frustrations. Or is it a specific issue related to my craft.
I unload the 4 prop guards to reduce weight but the same falling down situation does not improve.
Raymond
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