- Joined
- Jan 4, 2018
- Messages
- 33
- Reaction score
- 29
- Age
- 80
I have a very tiny vibration in my P3P.
I've balanced the props, the gimbal is fine, no looseness there.
I've clamped a pencil to each arm, barely touching the motor bell, then spun the motor.
Three motors leave a line all the way around but the fourth skips about half way round.
Was wondering what is the acceptable run out for these motors?
.001" or .002" would be acceptable, I think.
A question for the DJI office?
I've balanced the props, the gimbal is fine, no looseness there.
I've clamped a pencil to each arm, barely touching the motor bell, then spun the motor.
Three motors leave a line all the way around but the fourth skips about half way round.
Was wondering what is the acceptable run out for these motors?
.001" or .002" would be acceptable, I think.
A question for the DJI office?