Looks like, as you posted already that there must be some kind of homing, but not sure how that's done?
Bought a broken gimbal off ebay, replaced the board and motor of my gimbal with the one off ebay and now it works.
Anyone here ever just replaced the yaw-arm motor successfully?
Sent from my SM-G935T using PhantomPilots mobile app
Bought a broken gimbal off ebay, replaced the board and motor of my gimbal with the one off ebay and now it works.
Anyone here ever just replaced the yaw-arm motor successfully?
Sent from my SM-G935T using PhantomPilots mobile app