I posted recently about gimbal and RC link issues with my P3S; it’s a crashed drone I bought and repaired, replaced the gimbal board, yaw motor (rotated roughly), roll motor (had broken apart), and ribbon cable (had sheared), synced to RC by shorting the missing sync button, updated FW, calibrated compass and IMU, and took a successful test flight. Biggest remaining problem? Camera pitch is limp — not held steady automatically, doesn’t move in response to RC wheel. However, no relevant errors were reported by the DJI GO app at any point.
What’s most likely the problem? Pitch motor, pitch control board, ribbon cable, other? Is there any way to troubleshoot further other than trial and error?
ETA: Also, burned edge on the ribbon cable after replacing it, which I smelled but couldn’t immediately locate after a lengthy firmware update attempt.
What’s most likely the problem? Pitch motor, pitch control board, ribbon cable, other? Is there any way to troubleshoot further other than trial and error?
ETA: Also, burned edge on the ribbon cable after replacing it, which I smelled but couldn’t immediately locate after a lengthy firmware update attempt.
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