- Joined
- May 13, 2018
- Messages
- 139
- Reaction score
- 39
- Age
- 80
Have a recently acquired P4A with a IMU issue. PIcked it up from another P107 pilot thinning the backup equipment and am pretty sure he accurately described it a "low hours". Before discovering the IMU issue, I had replaced the the GL300C RC with a GL300F from a downed P4P with no problem to get increased range. IMU said it needed calibrating, so I did. After calibration, it shows "moving" when I check the health of sensors even while sitting static on a table, and when I power it up static in the driveway with no props, the location shown in Litchi slowly drifts even with a fairly steady GPS location. Did all the IMU re-calibration again as well as compass, and IMU still says it's drifting while it's static on my desktop. Is this likely to respond favorably if I keep trying to re-calibrate it, or have I got a repair issue?
Thanks for your thoughts.......... Bob R.
Didn't expect it to make any difference, but just to make sure, I re-linked the original GL300C RC, and the problem was the same with both controllers. I'll recalibrate the sticks just to insure there's not a stick input being received at the bird, but wouldn't expect a stick input to be considered in an IMU output.
Thanks for your thoughts.......... Bob R.
Didn't expect it to make any difference, but just to make sure, I re-linked the original GL300C RC, and the problem was the same with both controllers. I'll recalibrate the sticks just to insure there's not a stick input being received at the bird, but wouldn't expect a stick input to be considered in an IMU output.