Hi all,
I had a crash with my p4p. The yaw arm broke incl the flex cable and the flex cable of the yaw motor.
I replaced them all. But when I start the drone now it is facing to the left. When i push it to the right it takes a while to go back to the left position instead of going immediately. The ESC on the yaw arm gets really hot.
Also i saw this video:
Before i want to buy a new ESC board, is it also possible that the yaw motor is not working correct? Or are these problems all due to the ESC board?
Hopefully you can give me some advic
thanks in advance!
ps. also i got a gimbal overload message, which is flickering between normal and overload the whole time
I had a crash with my p4p. The yaw arm broke incl the flex cable and the flex cable of the yaw motor.
I replaced them all. But when I start the drone now it is facing to the left. When i push it to the right it takes a while to go back to the left position instead of going immediately. The ESC on the yaw arm gets really hot.
Also i saw this video:
Before i want to buy a new ESC board, is it also possible that the yaw motor is not working correct? Or are these problems all due to the ESC board?
Hopefully you can give me some advic
thanks in advance!
ps. also i got a gimbal overload message, which is flickering between normal and overload the whole time
Last edited: