Hi guys,
I updated the Firmware to v3.12 using the Naza-M assist 2.12
I'm wishing I didn't.
I use a Futaba t8j transmitter with its appropriate Rx fitted inside the Phantom.
All has been well with this setup for the last few months. No complaints, no glitches.
After the update - which all went great - I powered down, powered up, carried out an advanced calibration - all good, callibrated the sticks - all green, powered down and went outside to try. Did the Guinn-Step Dizzy-dance - successfully - and waited for the new light sequence to phase through. All settled quite quickly to a constant double-green.
I'm assuming this is normal - pre flight.
Arming the rotors - all good.
Throttle up over 10% and they stay idling - all good.
Increase to over 50% - no launch.
Through 60, 80, 100% throttle - nothing, continues to idle.
Input from the other axisses - pitch, yaw, roll - causes an audible increase in motor speed here & there.
So all signals are getting through (including throttle because it accepts the +10%unput) but nothing more than that.
Any ideas? I'm drawing a blank.
If anyone knows of a way to succesfully revert to the 2.02 Firmware is be gratefull to hear about that too.
Cheers, grounded and annoyed
I updated the Firmware to v3.12 using the Naza-M assist 2.12
I'm wishing I didn't.
I use a Futaba t8j transmitter with its appropriate Rx fitted inside the Phantom.
All has been well with this setup for the last few months. No complaints, no glitches.
After the update - which all went great - I powered down, powered up, carried out an advanced calibration - all good, callibrated the sticks - all green, powered down and went outside to try. Did the Guinn-Step Dizzy-dance - successfully - and waited for the new light sequence to phase through. All settled quite quickly to a constant double-green.
I'm assuming this is normal - pre flight.
Arming the rotors - all good.
Throttle up over 10% and they stay idling - all good.
Increase to over 50% - no launch.
Through 60, 80, 100% throttle - nothing, continues to idle.
Input from the other axisses - pitch, yaw, roll - causes an audible increase in motor speed here & there.
So all signals are getting through (including throttle because it accepts the +10%unput) but nothing more than that.
Any ideas? I'm drawing a blank.
If anyone knows of a way to succesfully revert to the 2.02 Firmware is be gratefull to hear about that too.
Cheers, grounded and annoyed